Hey guys!!
So, I recently picked up a little job from the local scrap yard. They wanted their skid-steer forks re-welded. I accepted the challenge, and brought the thing home.
This is what I started with:
So, I had my work cut out for me (no pun intended). I took it in to school with me on friday, and got the old weld out, after spending some quality time with the arc-air and a 7" grinder.
Then, I brought it home and started welding. I was running 5/32" 7018s at 210 amps on AC with the stickmate. I ran it at its maximum duty cycle for 6 hours straight, and it never missed a beat. The leads, electrode holder and the welder itself tho were all nice and toasty when I finally called it a night. I love that little welder, but I do wish I could afford a bigger one...
Anyway, I got up this morning early and took it in to the scrap yard. They were really happy with it, and watching them hook it up to the bobcat for the first time was the most nerve-wracking thing ive done in a while, because if that doesn't fit, it wouldn't be fun getting it back off of there. It slid right on, and the clamps worked like they should, and so its a job Im happy with. I asked them how they were getting along without it, and the guy said "we aren't". I got paid and now I think Im going back to bed. Or maybe i'll just drink some mountain dew.
So, here it is!! I did 10 passes on the top, and re-did all the welds on the bottom. I bought the biggest grade 8 bolts that I could find (1 5/16") and torched out a couple of holes for them, and put them in there. The top piece that mounts to the main plate was bent really badly, and I had to cut part of it in the middle just to bend it back to being straight. It was still too warped to weld the underside of it, however.
So, I recently picked up a little job from the local scrap yard. They wanted their skid-steer forks re-welded. I accepted the challenge, and brought the thing home.
This is what I started with:
So, I had my work cut out for me (no pun intended). I took it in to school with me on friday, and got the old weld out, after spending some quality time with the arc-air and a 7" grinder.
Then, I brought it home and started welding. I was running 5/32" 7018s at 210 amps on AC with the stickmate. I ran it at its maximum duty cycle for 6 hours straight, and it never missed a beat. The leads, electrode holder and the welder itself tho were all nice and toasty when I finally called it a night. I love that little welder, but I do wish I could afford a bigger one...
Anyway, I got up this morning early and took it in to the scrap yard. They were really happy with it, and watching them hook it up to the bobcat for the first time was the most nerve-wracking thing ive done in a while, because if that doesn't fit, it wouldn't be fun getting it back off of there. It slid right on, and the clamps worked like they should, and so its a job Im happy with. I asked them how they were getting along without it, and the guy said "we aren't". I got paid and now I think Im going back to bed. Or maybe i'll just drink some mountain dew.
So, here it is!! I did 10 passes on the top, and re-did all the welds on the bottom. I bought the biggest grade 8 bolts that I could find (1 5/16") and torched out a couple of holes for them, and put them in there. The top piece that mounts to the main plate was bent really badly, and I had to cut part of it in the middle just to bend it back to being straight. It was still too warped to weld the underside of it, however.